Back to Work: Outboard Repairs, Seacock Swap, and Stripping Out Bodges

Sorry for the radio silence! The last post went up back in July, and while the blog has been quiet, I’ve been anything but. Pretty much every spare moment since then has been spent working on the boat, and it’s amazing how quickly time disappears when you’re covered in Sikaflex or head-down in an engine.

The biggest milestone was finally getting an outboard sorted. The boat didn’t come with one, so this was a huge step forward. I found a good engine, gave it a full service, and even fixed a couple of issues: a blocked fuel tap and a snapped handle. Cleaning out the tap was easy enough, but the handle repair was a bit more creative. I drilled through what was left of it, dropped in a bolt, and sculpted a brand-new handle around it with epoxy putty. Surprisingly, it worked - and it looks half-decent too!

Next on the list was sorting out the sink drain. The old seacock was a corroded mess, so I swapped it for a TruDesign composite fitting. Thankfully, the skin fitting was still solid, so I reused it and sealed the whole lot with Sikaflex. This job was a nice reminder that sometimes you don’t have to replace everything, and that a little patience with sealant can save a lot of money.

The battery setup got a big upgrade too. The boat originally had a very tired 24V battery that was beyond saving, so I switched over to a 12V system instead. Twelve volts is much more universal, and it’ll make it far easier to add or build my own electronics later on without worrying about isolation or level shifting. I went for a 100Ah AGM battery from Halfords, which are basically rebadged Yuasa units. With my trade card, I grabbed it for £103 instead of £160

One of the nastier jobs was ripping out the old motor mount that the previous owner had “installed”. Picture untreated timber, badly shaped plywood, and some very questionable fibreglass work. The wood had rotted out completely, and the whole setup wasn’t even watertight. Worse, it blocked the plug designed to streamline the cockpit when the motor’s not in use. Removing all that felt like undoing years of bad decisions, and it’s satisfying to know the boat will be faster (and safer) without it.

Finally, I gave the whole boat a proper powerwash. It was deeply satisfying watching years of grime and mystery stains disappear in sheets of dirty water. She’s still very much a project, but it’s starting to feel like a boat again rather than a storage shed on a trailer.

Next time I’ll talk about some exciting new gear I’ve acquired - including a free wind system (thank you Don!) and the electrical overhaul I’ve got planned. Thanks to a generous tax refund, this refit has officially gone from “make do and mend” to “let’s do it properly”, and I can’t wait to show you what’s next. 

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